We removed the starter, alternator, heat exchanger and head (to reduce weight). Here the engine is separated from the saildrive.
Using a block and tackle jockeyed the engine into the cockpit.
This took three hoists, first with the boom to the cockpit coaming. Then to the cockpit seat and finally the cockpit floor using the bimini as a hoisting point. When we finally were able to remove the piston, we discovered that the top compression ring was broken in three and the second compression ring was shattered.
The piston itself was fractured between the rings.
Fortunately, there was a good machine shop on the French side called Mendall. However this meant that we had to strip the engine down to the block. Since this required a special deep well socket which I did not have, we brought the engine (using our grocery cart) to Simpson Bay Diesel where they were able to remove the governor nut. We dinghied the stripped down block over to the French side after Bastille day and they were able to bore and sleeve in one day.
Here is what the cylinder looked like after the sleeve was inserted.
We slowly put the engine back together, working out a detailed plan of what needed to be done, what tools were needed, torque specifications, etc. We were given a respite on Sunday due to the rain of the system that eventually become Bonnie. Two weeks after we started, we were finished with no extra parts and only three missing parts (which we later discovered after improvising replacements). The engine started better than ever and we decided to take a mini cruise to St. Barts to test the engine. So far all is working well.
Neither Simpson Bay Diesel nor Mendall had ever seen a piston with a ring as shattered as ours and they both suspected that it occurred during manufacturing or assembly. Since we had almost 2200 hours on the engine, it took quite a long time to show up. However, that engine had a persistent leak from the rear main seal (which was half out of the end cap when we disassembled the engine) and more curiously, the timing cover gasket blew out at the bottom and had to be replaced three years ago. So we may have always had a ring blow by problem that suddenly got worse in Antigua. Getting the engine out of the engine compartment is relatively easy and working on the engine in the cockpit worked out quite well. I took pictures of everything before I started and during the disassembly which proved invaluable during re-assembly. We studied that engine manual each morning before we started and planned each day in detail. I also used the parts manual to make sure we replaced all relevant gaskets, o-rings and copper washers. Having easy access to a Yanmar dealer and good machine shops was crucial to the successful resolution of our problem. Besides the sleeving, we needed to have the crankshaft bearings pressed in.
Here Pam is cleaning the engine compartment which is much easier with the engine removed.
